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ModelWorks
Foden
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Mounting Boiler in Chassis |
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Wednesday 19th November 2008: I have been putting off final assembly of the Foden for several years and today I finally fitted the boiler into the chassis. I found it easy to mount the boiler but as it has the potential to be a swine of a job I have written a detailed account.


Ever since the boiler was delivered it has lived on a 4 wheel trolley. This made it easy to move around the garage and it has done it job well. With the addition of cylinder, hornplates and motion it has become far to heavy to consider lifting.
When I built my Burrell I intended to buy an engine hoist to assist with assembly but fortunately after a chance remark to Steve he explained how to use bottle jacks. This was so successful that I decided to employ a similar technique for the Foden.
Yesterday I assembled the back axle and fitted the rear tyres. I had planned to place the chassis on blocks but as I found it so easy to wheel around I decided to wheel the chassis into the boiler. I calculated that with the boiler foundation ring approximately 250mm above ground level the chassis would be in alignment.
Unfortunately the
boiler was a bit low on the trolley and in order to avoid lifting it I
rocked it up using a bottle jack. Heres how:- I first jacked
up the front
pivoting on the foundation ring's back edge. This enabled me
to
change the front foundation ring support for a beam supported by blocks
on the garage floor. I set the height of these so that the
foundation ring was just touching. I then slowly lower the
jack
and since the centre of gravity of the assembled boiler is in froward
of the foundation ring the boiler comes to rest on the front foundation
ring support and the jack/front smoke box support. I then
added
more packing to the rear foundation ring support. Additional
packing was also added to the front so that the boiler would not have
far to fall should the jack fail. I then repeated this until
the
boiler was at 250mm on the front foundation ring support. It
is
harder to describe than do! It should be noted that the main weight of
the boiler at all times is on the blocks and daylight at the jack end
is kept to a minimum.
![]() The main boiler support was provided by a beam under the foundation ring with stabilizing support at the front |
![]() The chassis was surprisingly easy to move around on the rear wheels |
Next I rolled the chassis into position and tested the alignment of the chassis to saddle bolts. The alignment on one side was perfect but it required a slight sideways movement to bring the other side in line. The encouraging thing was that I had the boiler at the right height and I was able to loosely insert 3 of the bolts on each side.
I then loosely fitted the 4 hornplate chassis mounting
brackets to the chassis and it looked as if my luck was running out.
The mounting holes in the bracket did not align with those in
the
hornplates. Since I have
previously fitted the boiler
to the chassis I knew that all the holes would align provided
I
had the boiler in just the right position. The back of the
boiler
was slightly too low and by using jacks under the beam supporting the
foundation ring I was able to adjust the packing to bring the rear of
the boiler into perfect alignment with the chassis mounting brackets.
I now had the boiler supported in exactly the right position
and
it was just a matter of fitting and tightening all the mounting bolts.
The next task was to remove the trolley and prepare for the fitting of the front axle. Using a version of my rocking technique I adjusted the support packing so that all the weight was taken by the beam supporting the foundation ring and the rear wheels. Since there was now no weight on the trolley it was simply pushed out of the way. I then temporally rebuilt the packing under the boiler saddle (on the garage floor) and by jacking the rear of the chassis was able to remove the weight from the beam under the foundation ring. This enabled me to rebuild the packing directly under the foundation ring ready to mount the front axle.
While this account may appear long winded it only took half a
day and I personally never lifted the boiler.
Thursday: I got on and fitted the front axle today supplied in kit 2. Since the tie bar from the axle back to the boiler are an essential part of the axles support I decided to fit these next. This should have been a simple job but I caused myself a lot of grief, see kit 17.
I
was concerned that the tie bars would prevent the axle rocking so I
decided to check this out. With the aid of my bottle jack I
simulated one wheel falling into an extreme pothole.The axle passed
with flying colours.
Friday:
Having got over yesterdays blunder I fitted the front brakes and
assembled the steering. I am now waiting for the loctite to
set
before fitting the front wheels.
Saturday:
Fitting the brake drum took a little longer that it should due to an
oversize hub. See kit 5.
Weekending
Friday 28 November: I
took things at a leisurely pace this week. I have
now
fitted most of my stock of painted parts and will soon have to start
opening boxes containing untouched kits. I have dug out kit 12 and plan to trial
fit the brake accessories.
Monday: I spent today curing an
annoying metal on metal rub withing the left front wheel. At
first I put this down to the brake shoes but when striped the hub down,
removed the brake shoes and reassembled it the rub was still present.
In the end I tracked the problem to the rim of the brake drum rubbing
on the backing plate (in the outer grove). The bake baking plate
appeared warped at the point at which it rubbed the drum. I
tried to deepen the grove in the backplate using a cutting in my mini
drill without success. I then removed the backplate and tried to
flatten the backplate again without success. In the end I
resorted to mounting the backplate in my lathe and remachining the
grove so that it was true with the backplate's fixing. I then
reassembled the hub, without the brakeshoes and was rewarded with a
wheel that would turn without any hint of rubbing. It is clear
that a lot of fetling is required when assembling the front hubs but
the alternative is to put up withgrinding noises whilst driving.
Tuesday: Today I have been working on front mud guards supplied in kit 12
which led me to ponder the strength of the saddles fixing bolts.
I have been uneasy as to the strength of the 6 M5 bolts which
Modelworks use to attach the boiler saddle to the chassis. When
tightening these I have had to hold back on the applied torque as I am
very conscious how easy it is to sheer a bolt.
The Rex drawings show these as 1/4" BSF and M6 would make a
better substitute. The data tables show that the effective cross
section of a M6 thread is 14.2 mm2 as opposed to 8.8 mm2 for M5. This is backed up by my tests
which demonstrated that M6 bolts are nearly twice a strong as M5.
It turned out relatively easy to drill out, retap, and replat
each bolt in turn with an much stronger M6. Fitting of the mud guards is described here.
continues
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