Third Steaming
Tuesday 4 April - Success Day
ModelWorks 4 inch Scale Burrell Agricultural Traction
Engine
Tuesday: I hope to take the Burrell for it's steam test on
Sunday and today's exercise was to prove that everything is ready.
Transport to the test site is essential so I took the Burrell for a short test drive. I am relieved
to say that the trailer and load behaved itself. I got a
bit too relaxed and took some speed bumps a little too fast and the
trailer went airborne (speed about 20mph). On the plus side
this confirmed the lashing and suspension of the
trailer.
I used to own a house with open fires and a coal fired Rayburn.
When this is your main form of heating you get quite skilled at making
and maintain fires. There is much hot air expended on how best to
light a Rayburn but the truth is that it is best to adopt a style that
works for you and your Rayburn. Previous when firing the Burrell I
tried to slavishly follow other peoples advice. While this was relatively
successful for this steaming I decided to follow my own instincts.
After all the Burrell's fire box is about the same size as my
old Rayburn.
A
friend has found an excellent source of firewood in the form of rough
wooden crates thrown out by a local firm. This timber is dry and appears
to be untreated. Since this has always been my preferred method of
ignition I decided to dispense with the barbeque charcoal and use wood
instead. I never used Paraffin in my Rayburn and as I believe
this is responsible for much of the smelly smoke I used the wood dry.
I did however dip one or two small pieces of in paraffin and after
lighting these on the shovel I dropped them onto the kindling already in
the fire box. I added a few more pieces of dry kindling closed the
firedoors and waited.
I
could see through the crack in the firedoors that the wood was catching
and I was pleased by the reduced quantity of smoke issuing from the chimney.
What's more it was less smelly.
The fire was more controlled and did not burst out of the firedoors
when they were opened to add more wood. Over the next hour I
slowly built up the fire adding smokeless coal every five minutes or so.
After about Ninety Minutes the safeties lifted. At 120
psi they were only hissing but by 121psi a plume of steam was reaching
up to the top of our four story house. There pressure did not rise
any further. As the pressure dropped the safeties required a
gentle tap to reseat and stop the flow of steam.
Having used up some water it was time to test the two methods water
feed needed for the test. I closed the pump bypass and I am
pleased to report that it worked. PTFE appears to be a good
replacement for the O-rings but I did have to shorten the pump gland to
enable the 3 C's of PTFE to fit comfortably.
After confirming that water was going up the glass I opened the pump
bypass and tried the injector. Since my last steaming I have
removed the filter and this has made it easier to get the injector to
pick up. Throughout the remainder of the steaming I used both the
pump and injector to maintain the water level with total success.
I was pleased to find that the fire was much more controlled and I
suspect this was in part due to not using Barbeque charcoal.
Previously I used a fair quantity to light the fire and I suspect it maintains its heat for a long time.
Steve
Traill has successfully modified his water lifter. Since his
modification is relatively drastic involving changes to both male and
female cones I decided to try a simpler modification. I made a new
female cone with slightly steeper cones. Unfortunately this did
not work and in an attempt to discover the source of the problem I
removed the lifter from the tender and set it up to blow water across
the garden. My experiments showed that the lifter only worked when
the water source was raised above the lifter.
Steve Traill has explained his modification to me and for my next
steaming I will try and follow his lead.
As
the day progressed I became concerned by an annoying click coming from
the motion. After a thorough investigation I concluded that it was coming
from or near the pump eccentric. As I could not investigate this
further whilst in steam I made a decision to stop adding coal to the
fire.
I let the engine stand maintaining the water level with the injector;
it did not need much. After ninety minutes when the fire was no
longer showing any life I dropped the firebox.
For the first few steaming ModelWorks have recommended that the
boiler is completely blown down after each steaming to rid the boiler of
any foreign matter. I am beginning to wonder if this is necessary
as each time only clean water emerges and the engine shows no tendency
to prime.
I am very pleased with today's steaming. I felt in control
throughout and am looking forward to my trip to the park on
Sunday. With the fire under control I found I used much less water
and the tender float was a great success. I have some work
to do before Sunday, most importantly to investigate the click
from the pump eccentric. A quick look this evening suggests that
the pump eccentric is being twisted by the pump's connecting rod and
this is the first thing I will check tomorrow.
Wednesday: When I refitted the pump after fixing leaks I had
forgot that the connecting rod fitted one way better than the other as
the mounting holes had been drilled slightly off centre. Rotating
the connecting rod improved things but to make sure I removed the pump
and elongated the mounting holes slightly. This enabled all twist
to be removed from the eccentric.
Examining the inside bore of the piston I was surprised to see dents
caused by the connecting rod hitting it. Could this have been the
source of the click? To ensure no contact I filed away the connecting
rod in the region where it emerges from the inside bore of the pump.
I had a chance to examine the PTFE packing and it looked the business.
I am sure this is the right solution. I believe I now have all the
Burrell glands packed with PTFE C's.
Thursday: Having
completed the essential repairs I set about making replacement cones
for the water lifter. Steve Traill had sent me a drawing of a full
size Clayton & Shuttleworth water lifter which he used as the basis
for his successful replacement.
As
I have not yet modified the water lifter's steam cock I decided to scale
the full-size lifter down by a factor of 3.5 in the belief that this
would make it less steam hungry. The notable differences are that
it is has a steeper cone on the inlet side, the minimum diameter is much
less and is much longer.
My first job was to modify the male cone through which the steam is
blown. As supplied it had a tiny hole and I opened this out to
1.4mm. To smooth the flow of steam I stepped drilled in from the
steam pipe end using 1.7mm and 2mm drills. The full size had a
hole size of 5mm with a steady taper out to 12mm for the steam
pipe. In the full size the tip of the male cone was position 25mm
away from the female cone but Initially I am leaving it at it current
length which means it tip is inline with the start of the female cone.
Before I could make the female cone I had to make tapered D bits in order
to cut the cones. I have made several of these before from Silver
Steel but never any this long. I made the cutters slight
longer than necessary so that if necessary I can Increase or decrease
the diameters. The outlet cone is long and has a very shallow
taper and it was a bit tricky to mill the flat on the cutter. Once
complete I harden and tempered the cutters though for a one off in brass
I might have got away leaving them soft.
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Milling the cutter's "D"
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The completed taper D bits
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Once
the cutter were made it was relatively straightforward to make the new
cone. I roughed out the cones by step drilling finishing to size
using the tapered D bits.
I reassembled the water lifter and before refitting it decided to see
if it would work on compressed air. I was very pleased to find
that it did and it had enough suck to pull water up the full
height of the delivery hose (2M). I was a bit disappointed with
the rate of delivery of water but I imagine that it will be much better
on steam.
Steve Baldock has just contacted me to say that ModelWorks will be
supplying replacement cones for the water lifer based on Steve Traill's
research. There will be one or two other goodies and these
will be manufactured and dispatched as soon as they can be slotted into
the factories busy manufacturing schedule.
Sunday: Today I took the Burrell to my
local club to get it tested. The testers decided to conduct both a
hydraulic and steam tests. The hydraulic test sprang leaks I
never knew I had. As part of the new test code it is necessary to
establish the capacity of the boiler so the boiler was drained down into
a measuring jug. For the record the capacity was determined to be
26 liters.
Raising steam took exactly one hour from lighting though it felt much
longer. The safety valve was checked first. After building a
very generous fire the blower was turned on until the safety valve
lifted. The distressing part is that the test continues until the
testers are satisfied that the pressure will not rise any further.
I was relieved when the blower was closed and the test past.
Next came the water feed arrangements. The pump worked though
it was suggested to me that the pump efficiency was being reduced by
bouncing ball valves. The injector was not on it best behavior
needing continual tweaking to keep it working.
With the test successfully completed I was persuaded to go the
long way round the club track to avoid a short steep hill. This
was my first chance to drive any significant distance. My
education started immediately when the engine started to prime.
Either it was me, the motion of the engine or stuff dislodged by the
test but the engine primed several times during my circuit. Each time I
had to stop and recover the water level. I used about 50 liters of
water to go less than 1 mile.
I tried my modified water lifter and while it worked it was not a efficient
as expected. It took about 30 seconds to empty a bucket of water.
Tuesday:
My NTET disc came through today and I must congratulate Walker
Midgley on their excellent service. This will come in handy as
I am hoping to go to my first rally this weekend. With the
prospect of a rally this weekend I wanted to get on and attend to the
snags uncovered on Sunday.
It was suggested to me that the crank pump efficiency was being impaired
by the bouncing of the balls inside the pump as a result of excessive
lift.
I can now remove the pump in my sleep and my first act was to measure
the ball lift. The inlet ball had a lift approaching 1/4"
whereas the outlet ball had a lift of around 3/16". Since
these lifts were greatly in excess of the 1/32" recommend to me
decided to have a go at reducing them.
It
was relatively easy to limit the rise of the outlet ball. I simply
drilled and tapped the pumps top cover and made and screwed in a brass
button. I then trimmed this to give a rise of 1/32".
The inlet chamber presented a few challenges. The biggest was that
it's roof does not present a even surface to act as stop for the ball.
My experiments showed that when the ball hit it, the ball was pushed
sideways. In the end I decided to improve this as much as I could using
my mini drill. Making a new inlet bush was straight forward except
I had to allow for the fact that the chamber was not tapped to its full
depth.
I have now reassembled the pump after checking that the ball lifts were
1/32". When I next steam it will be interesting to see
whether these changes have made any difference.
Wednesday: I am still having trouble with the bolts coming loose
on the reverse reach rod and on Steve advice I have
decided to weld it up. I carefully set the length of the reach rod
so that the die block did not knock in either forward or reverse
settings. Removing the reach rod whilst full assembled was
tricky. After removal of the injectors steam feed pipe I was able
to jiggle the reach rod out backwards. With the bolts still in
place I welded the parts together and then removed the bolts and welded
up the holes. Once I had cleaned up and filed away the excess weld
the reach rod looks as if it was made in one piece.
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