Second Steaming
Monday 20 March
ModelWorks 4 inch Scale Burrell Agricultural Traction
Engine
Monday: I attempted to repair the pump last night. When
I refitted it I was frustrated to find it was leaking from the original
spot. Without much hope of success I removed the pump and stripped
it ready for my fourth re-brazing attempt. When I refitted it the pump
body did not leak. A victory but read on.
Encouraged by this I decided to try my second steaming.
I got on much better lighting the fire. I momentarily dipped a few
bits of kindling wool in paraffin and I put this together with some dry
wood into the firebox. I lit a small bit of kindling wood on the
shovel and dropped it in and closed the doors. After a few minutes
I added some larger kindling wood. Over the next hour I slowly built up
the fire adding a little coal every 5 minutes. As the picture on
the right shows it is essential to keep the fire doors closed.
It
took about an hour to reach the point where the safety valve began to
lift. I found that the safety valve lifted at 110 PSI rather than
the expected 120 PSI. I will get the gauge checked but I suspect I
will need to adjust the safety valve.
All
this blowing off used up some water so I decided to use the pump.
As the picture on the right shows it sprang a leak. The good news
was the leak was not from the pump casing. What appears to be happening
is that water is escaping past the o-ring and spurting out between the
pump body and the gland packing. I have contacted Steve in the hope that
there is a simple solution.
There was good news when I tried the injector. It works!
I turned on the water and as I open the steam valve water spurted
out the overflow but as I open it further the overflowing water reduced
to a dribble. I then trimmed the water valve and got the water
going into the boiler with the overflow dry. Over the next hour
the safety valve periodically blew. I did not add any coal to the
fire, closed the damper and used the injector as much as I could.
For stationary running I had built far too big a fire.
Misfortune struck as dirt got stuck in the injectors clack
valve. I tried running the injector to clear the crud but the
steam being blown back to the injector heated it too much and it refused
to pick up. I was glad that the clack incorporates a cock and I
turned this through 90 degrees to isolate the injector. I now had to
rely on the crank pump.
By now the fire was cooler and the pressure was begging to
fall. The pump spurted more water than went into the boiler but
the water was going up the glass. I ran for another hour
maintaining the water level using the pump. By keeping a very mean
fire I was able to hold the pressure at 50 around PSI. The fire
bed was only about 3/4" deep with a few larger lumps.
The engine ran very well and I believe it is starting to free up. One
job I shall add to the "to do list" is to remove the shims from the eccentrics
as they were a bit slack.
I
stopped putting on any more coal but the engine ran on for another 1/4
hour.
Last time I had to drop the fire in a hurry and I could not find
anything to drop it into. In desperation I used a sheet of Aluminum
but had difficulty keeping the hot coals away from the wheels.
I have now made a "product improvement" and folded this
into a large tray. This worked very well with the added bonus that
I could drag the fire out from under the engine.
My second steaming was successful. I am sure the injector works
despite my problems with the clack valve. I am beginning to learn
about the fire and I shall be meaner on the coal in future.
Even the pump is showing encouraging signs.
Tuesday: After
my PHD thesis in lubricator linkage geometry
I have decided to refit the original lubricator supplied by
ModelWorks. Having used a ratchet based lubricator I now
know the strength and weakness of both. I believe the ultimate reliability
of the ratchet is superior but roller clutches will work with a small
arm movement. I changed because I was a bit short of arm
movement and ModelWorks have improved the reliability of their
lubricators by increasing the diameter of the operating shaft.
Wednesday 29 March: I have been very busy recently sorting out a
trailer to transport the Burrell. I have not yet had time to implement
the fix for the leaking pump. It would seem that I am not the only
one to experience water leaking past the pumps O-ring. The easiest
fix is to fit a second O-ring but after discussion with Steve I
have decided to try replacing the O-Ring with 3 rings of 3mm square
section PTFE yarn.
In
choosing a trailer to transport the Burrell I have been forced to
compromise. If I had a large tow vehicle and plenty of storage space I
would have gone for a twin axle covered trailer. Unfortunately I only
have a Rover 25 and no storage space. Having had some
previous experience of towing I ruled out trying to get a small light
unbraked trailer. In any case keeping the gross weight below
750Kg would be difficult. Opting for a braked trailer only increases
my cars towing limit to1000Kg but makes the towing experience less
exciting. The down side of a braked trailer is that they are longer and
heaver that their unbraked counterparts.
For reasons I am now questioning I opted for a platform trailer from
Benderup. I chose is the discontinued Bravo 225
which has a bed size of 2.2M x 1.4M. The advantage of this trailer
is that it weights only 250Kg and has a maximum width of 1.54M.
I was soon to discover a big down side namely the loading height.
My original concept was to tip the trailer up to bring the back near the
ground and with a short ramp run onto the trailer. When I got the
trailer home I fitted an extra long prop stand at the front and tipped
the trailer. As it looked very scary I abandoned this idea and
began to wonder why I had brought a trailer with a 0.6M loading height.
I decided to follow conventional wisdom and load with the bed
level with prop stands at the back to stop the bed tipping. Research indicated that I should aim for a maximum ramp
gradient of 1 in 3 so I needed 2 metre ramps.
As supplied there was no suitable place to fit a hand winch. I
had hoped to buy a suitable winch post but as none was available I was
forced to make my own. Welding is not one of my skills but after
making a prototype I was able to weld up a reasonable winch post.
The horizontal tube reacts the load directly to the bed of the trailer.
Once
I had fitted the winch I was keen to try and load the Burrell. I
positioned the Burrell at the foot of the ramp. I unwound the
winch cable and attached it to the front tow hook and began to
wind. Instead of the Burrell moving the cable started to tighten
and kink on the winch drum. Before trying again I shortened the original 15M of cable
such that it was fully unwound with the Burrell a few inched from the
base of the ramps. This ensures that there is no slack cable on
the drum at the start of the pull.
As
I had a single axle trailer I needed to position the Burrell so that the
nose weight was correct. I am sure I am not the first to use
bathroom scales but they made a very effect nose weight gauge.
With a bed 21 inches longer than the Burrell I had plenty adjustment
but the correct position turned out to be with the Burrell roughly in
the middle (1.5 inches back from centre). I will need to repeat
this excise with the Burrell wet. My guess is that with a dry
tender and a wet boiler the Burrell will be in the middle. The C
of G of the dry Burrell turns out the be roughly 12 inched in front of
the rear axle.
Friday: Yesterday I fixed strong hooks to each
corner of the trailer plus the centre back and front. I
used an extra strong fixing at the back of the trailer as this will take
the main load during braking. My original plan was to attach a
chain between this and the Burrell's rear tow hook. When I
fitted this I found that it was more vertical that horizontal and hence
unable to do its job properly. Instead
I placed a strop around the bottom of the smoke box and ran a lashing
under Burrell back to the rear fixing. To prevent rearward
movement I attached a strap between the Burrell's front tow hook and the
front of the trailer. As I am nervous of the Burrell moving I
placed addition lashing around the Burrell rear wheels. I need to
do some more work on these as I am not convinced I have fitted them
correctly. I would also like find a way to utilize the Burrell's
rear tow hook as this might enable me to dispense with the wheel straps
all together.
I
could now turn my attention to preparations for my next and hopefully
final steaming before my steam test.
My first task was to fit 3 C's of PTFE packing to the water
pump. I am using 3mm square section PTFE woven yarn available from
LSM. In
order to cut the C's I wound the yarn around pump's piston and cut
the rings in one go using a scalpel.
To fit the rings I temporally inserted the piston and pushed the PTFE
into place, staggering the joints.
The
three rings filled most of the space previously occupied by the
pump gland. It might have been better to only fit two rings but as
I was determined to stop the leak I stuck with three and will fit longer
studs.
I shall have to be careful when tightening the gland not to twist it
and jam the pump's piston.
Saturday: I started by refitting the pump. Finger crossed that
it works.
I turned my attention to the safety valve. I had contacted
steve an he advised that I should try 1/3 of a turn on the adjustment
nut. This is located under a brass cap that is held in place with gasket
paste.
I took the opportunity to fit longer studs to the cylinder as the originals
for the safety were a bit short.
In
the process of removing the safety valve I destroyed the gasket.
ModelWorks originally supplied a spare but as I had already used this It was time to make some more. Fortunately I had some
1/16 thick proper gasket material that I had previously brought from
LSM.
I have made several sets of gasket for my POP and I have achieved
good results printing the outline using a inkjet printer. The
image on the right links to a graphic which should be printed at
300dpi. As a cross check, check the outside dimensions of the
gasket.
If the gasket material was paper based I would printed directly onto it
but as the material was graphite loaded I printed
on ordinary
paper and stuck it to to gasket using spray mount adhesive. Do not
use water based adhesives as they will alter the size of the
paper.
I cut the outline using a scalpel but for the 6mm holes
I use a home made punch. I have made several of these and each
consists of a C shaped body with a hole for the punch. The punch
is made from a length of silver steel with the intention of hardening it
but I never have. For these 6mm holes it may be possible to use a
stationers punch.
Monday:
On my first steaming I found it very difficult to gauge how much water
was in the tender. The the try cocks on the side of the tender are only
able to indicate completely full or nearly empty. Steve Traill has
fitted a dip stick to his tender and for my second steaming I made and
fitted one also. While I was able to determine how much water was
in the tender it was difficult to read the mark on the dip
stick.
For my third steaming I have made a float. This should be easier to
read and should enable me to dynamically see the changes in level when
using the injector.
I
wanted a thin float that would act in line with the rod to minimize the
chance of it sticking. The prototype float is made from expanded polystyrene
and if successful I plan to make a more refined version. I
used a heat gun to seal any loose polystyrene though I might also
give it a coat of paint but first I have to find a paint that won't dissolve
the polystyrene .
The level is indicated by a 1/8 stainless rod that runs in a brass
bush fixed to the tender. To drill a hole 1/2" out from the
tender side I had to Loctite a drill into a length of bar stock.
How
I never lost the lubricator cap for my POP I will never know since it is
extremely easy to knock off. It probably was tell tale tinkle as
it hit the floor. Since I am now going to stick with the
ModelWorks lubricator I decided to remake the cap. Some
constructor attach the cap with a short length of chain but I went for a
more elaborate solution.
I milled a new cap and hinge from 3/16" thick brass bar
stock. Now that I have fitted it I am very pleased with the
improvement in appearance. When I get round to repainting the pump
I think I will paint the lubricator at the same time.
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