First Steaming
Monday 13 March
ModelWorks 4 inch Scale Burrell Agricultural Traction
Engine
My garden is not the ideal place to steam the Burrell since there is
no suitable flat area. My drive slopes at 1 in 6 and in
order to level the Burrell I have had to made a ramp to support the back
wheels.
I tried lighting the fire using barbecue brickets soaked in
paraffin. Unfortunately I left them soaking much longer (days)
then recommended by Steve and I ended up with more paraffin than
could be burnt by the available oxygen. Even if relit it was going
out in a few seconds.
All I had was a smoke
generator so I dropped the fire and started again.
Having stunk out the neighborhood I went back to using
wood. I
started with a few small sticks soaked in paraffin (normally used for
the POP) and some larger pieces of dry timber. I built the fire up
slowly adding more wood. I was soon able to add coal and I
continued building the fire without any further problems.
I did notice a dribble of water from the smoke box but as Steve
warned this might happen I did not panic and after a while it stopped.
After about an hour there was 50 PSI on the clock and I decided to
give the engine a run. With the drain cocks open it started first
time.
I left the engine gently ticking over and I continued to slowly build
the fire. After about another half hour I got to 90 PSI and as the
water was now less that 1/2 a glass I decided to try the crank
pump. Unfortunately it leaked.
With the crank pump out of action I tried the injector with only limited
success. I did manage to fill up the boiler but the injector only worked in
fits and starts.
I have talked these problems through with Steve and I understand that
more modifications to the injector are needed. The good news is
that Steve Traill has already incorporated the mods and passed his Steam
test last Saturday.
The problem with the pump is down to faulty brazing and I am debating
whether to have a go fixing it myself or sending it back for
repair.
I had deliberately built up the fire slowly and after about two hour from lighting the fire the safety valve blew.
The rear safety continued to
blow despite the pressure dropping to 70 PSI at which point I
decide to manually reseat it.
Blowing off used up some water so I tried to replenish it using the
injector. As I only had limited success at this and I was becoming
suspicious of the water gauge I decide to call it a day and drop the
fire.
I
had not planned to drop the fire and did not have a suitable tray to
hand. I pressed into service a sheet of aluminum but I had to quickly
knock the hot coals away from the wheels. Before I steam
again I will fold up the sides of this sheet so as to provide protection
for the wheels.
I did drive the engine a short distance up my drive. To
my surprise the front wheel refused to steer. Even when I got off
and walked alongside the engine it would only go in a straight
line. My best guess is that the 1 in 6 slope was loading the
differential so much that it was jamming. I hope this will improve
as the engine is run in.
Tuesday: Looking back over yesterdays steaming it was quite
successful.
A lot more could have gone wrong and I am thankful that I had no
significant leaks.
Thursday: Steve has been busy at ModelWorks
and solutions to the injector problems have been devised. It turns
out that Steve was over generous with the size of the injector
specifying a 8 pint/minute injector. Unfortunately not enough
steam is reaching the injector to satisfy it's appetite. The
solution is to modify the injector steam cock to increase the size of
the internal passages so there is less of a restriction to the steam.
Customers will shortly be getting a letter asking for the return of the
injectors globe valve body and both clack valve blanking plugs for
modification. A lesser problem affecting the injector is the
water supply and it may be beneficial to remove the filter so as to
increase water flow.
Having discussed the modification to the globe valve with Steve I decided
to tackle this myself. This is not for the faint hearted and all
but the best equipped should return the cocks to Modelworks for
Modification.
Each end of the valve body is counterbored with a 3/8" slot
drill as deep as possible without breaking through. This leave a short
section of the original steam passage and this is elongated with a file
to increase its capacity. The valve seat is not modified in anyway and great care is needed when enlarging the holes not to disturb it.
The
easiest way to remove the valve bodies was to remove the steam
head. When I was undoing the pipes I had problems with the globe
valves turning. When it came to refit the steam head I devised a
very effective way of holding the globe valves still. I threaded a
length of brass bar 3/8" x 32 and screwed it into the vacant
position normally occupied by the tap assembly. This worked extremely
well as I was able to apply force between the bar and spanner without
any hint of movement of the body. I had to be careful not to
overdo it as it is possible to snap a fitting if it is over tightened.
I originally planned to return the pump to ModelWorks for repair but
having talked this through with Steve I decided to have a go myself.
During manufacture the pumps were held together with internal pegs and
tight fitting bushes so it is possible to reheat it without it falling
to pieces.
I removed all the paint from the pump body and mechanically
cleaned around the affected area and applied flux. Using a
relatively powerful torch I heated the pump and ran in silver solder to
the location of the leak. This went very well and I was happy
until I dropped the pump from the brazing hearth onto the floor.
Even
though it only fell a few inches sods law applied and it landed on the
threaded bypass boss. At this point I really wished I had returned
the pump to ModelWorks.
 
Even though I had previously agreed with Steve that ModelWorks would
replace the pump if it went wrong I was determined not to be beaten.
I had a similar accident with my Kite spray gun and was able to
pull back into shape.
The
dent was only affecting the top 1/4" and I needed to find a way of repairing
it without damaging the bore lower down where the "O" ring
sealing the bypass cock runs. I made a brass collar to slip over the
boss and a moon shaped wedge to go inside. Using a small tool
maker clamp I was able to pull out most of the dent.
The bore was beginning to look salvageable but tests showed it was a
few thou out of true and the bypass cock would not fit. I made a
former which I used to grind down the high spots.
 
My efforts were rewarded when I got the bypass cock to fit. The
only remaining problem was the thread. I could not get my
9/16" x 26 die to engage so I cleaned the thread up the best I
could with a thread file. This is a special file with serrated
teeth that cut groves to match the tread form. I was then able to
engage the die and run it over the thread. As the picture below left
shows it nearly looks as good as new.
 
When I first saw the damage I thought the pump was only fit for the
bin. Now that I have cleaned up the pump and repaired the damage I
am happy again.
The re-brazed seams look good but I will not know for sure until I
refit and test the pump. Saturday: I
refitted the water pump today. I decided to test the pump running
on air rather than steam. I filled the tender with water and used
my compressor to pressurised the boiler to 50 PSI. When I
closed the bypass I was disappointed to find another leak.
This time the leak was on the top of the pump where the main pump bore
joins the clack chambers. The leak was shooting a very fine filament
of water high into the air. The leak may have been there all
along but did not stop the pump working. When I finished the test
and blew down I was surprised how much water was pumped into the boiler. When
I removed the pump and inspected the leaking seam under a magnifier it
looked perfect. Using a scriber I excavated the steam and found a
small blemish under the surface. In preparation for re-silver soldering
I used a small burr in my mini drill to open a thin trench around the
affected area. I returned the pump to the brazing hearth and it
did not take long to run in some more silver solder. I hope the
pump will be OK now. One comment I received from Steve is now
making more sense. He said that many pumps can be fixed by just
reflowing the existing silver solder.
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