Tuesday 10th January 2006: The arrival of the of the safety
valve today is a bit of an anticlimax as I am in no hurry to steam the
Burrell. For once I will not be amongst the first with news so if
you have steamed you Burrell, successful or otherwise, please let me
know and I will share you experiences on the web.
send report to:
The main reason for my delay in steaming is that I am waiting for the warmer
weather. It also seems silly to get the boiler wet in the middle of the
winter when the normal practice would be to lay it up dry for the winter.
I am pacing my self so that I can get a few steaming under my belt before a
boiler test and then straight into the rally season.
As well as the safety
valve the kit included the makings of a leather belt for the governor, the safety
glass for the water gauge, the seat's base plate and a mystery grub
screw. The note with the grub is not much use as no instructions were
included. I have just heard from Mike and this shipment did not included
the gauge cocks for those customers who returned them for repair.
Apparently they are waiting but need to be claimed!
While it would be tempting to polish the safety valves I have had a good look
at my full-size picture archive and black paint appears to be the norm.
Many miniatures leave the top section of the cap bare and polished but I can't
find any example of this in full-size.
Thursday:
I have now painted the safety valve with high heat gloss. This
was made more difficult as it was not appropriate to dismantle it as ModelWorks supplied it preset and tested. Yesterday I carefully
masked of the operating lever, ports and spring and gave it a coat of etch
primer. Today I spayed it with the high heat paint and am now
waiting for it to dry. I also painted the seat's base plate.
Debbie
answered my grub screw query; apparently the grub screw is to replace the one
in the regulator nut as it is believed to foul the bottom of the safety
valve. I have had a quick look and my grub screw does not come up much
past the top of the nut.
Since the paint is still wet I have not been able to try
the safety valve in position but I suspect it will clear the bush on the
underside of the valve. I wonder if the control model had an extra
long grub screw fitted?
Friday: Now that I have the gauge glass I could sort out the
length of the protector. I had previously counter bored the
top plate to allow it to clear the top nut but I was still having
difficulty fitting. Today I ground about 25 thou from each piece of
glass and shortened the rods by a similar amount. This has made
fitting easier.
I think the cause of the difficulty is the variability of
hornplate alignment relative to the boiler discussed in kit
12. The top cock is secured to the 2nd shaft which takes it
datum from the hornplate whereas the lower cock is fitted directly to the
boiler. As my hornplates are lower that the nominal position I have
a slightly shorter gauge glass. There could well be someone other
there who finds the gauge glass protector too short!
I have just tried the safety valve in position and the original
grub screw does not foul the bottom of the safety valve. I am puzzled
as the replacement screw was slightly longer! I shan't worry any
more about a problem that I haven't got.
I probably won't permanently fit the governor belt which
is just as well as it is slightly too wide.
I could finally fit and try out the seat. The foot rest would be in
just the right position except that the winch rollers get in the way of my
leg. I found it more comfortable to sit with either one or both feet
inside the tender but I suspect this will not be appropriate once steam is
raised.
Over the next few day I plan to search through my kit
residues and fit all the remaining items.
The first
job I tackled was the fitting of the cylinder drain pipes. These
pipes were supplied unbent and it took me a while to get the bent to an
correct shape. The pipes are held in place against the cleading
using a clamp secured to a plate on inside of the cleading. To avoid
any problems I had previously Loctited this plate in position prior to
fitting the cleading. This worked well and I was able to fit the
pipes with ease.
Monday: Over the weekend I trawled through
all my kit residues and fitted the few remaining parts. I have been troubled by the operation of the regulator
since fitting it in kit 20. - It needs to be
pull backwards to go. Whilst at Dorset I snapped Burrell Road
Locomotive YA 366 which had a regulator similar to our Burrell. Note:
shut is fully back
I believe this is more intuitive and wanted to follow
suit. This is easy to accomplish by changing the position of the
side valve on the regulator operating rod but first I needed to file a new
notch. I took the opportunity
to make new notch bigger as I have been finding difficulty setting a slow
idling speed.
This
afternoon I struggled to find anything else to do and so I must conclude
that the Burrell is finished. To celebrate the occasion I took a few
photos inside the garage. Here is another view at high resolution 1600x1200.
I don't intend to do any more until the spring when I will
give the tender and boiler a good wash out, test the axle pump and then
steam.
Monday 30:
Even though I have now got the original lubricator working
I am nervous about the long term reliability of the roller
clutches. The POP lubricator was temperamental until I discovered
the need to prevent the build up of "oil gunge" inside the
clutches. I found the quickest way to dislodge this was a quick
blast of WD40. Whilst at the Ally Pally exhibition I
purchased a new lubricator from the stand of RA
Barker. The new lubricator is slightly bigger and will not fit on
the existing mounting bracket. While I could have extended the
existing bracket I decided to machine a new bracket from BMS; shown part
completed in foreground.
Also on RA
Barker's stand I noticed a nice pair of 4" scale "King of
the Road " lamps. As lamps are only decoration I could not
justify the expense but seeing them has inspired me to consider making
some. From a search of the web (e-bay!) I determined that typical full-size
dimensions are 12" high including handle with a 4" base
diameter. Even though the brass will be expensive, next time I go
to the right shops I plan to buy some suitable chunks and in the mean
time I shall be on the look out for full-size examples to photograph.
Friday 3 Feb: The oil deliver rate of the new lubricator is
adjustable. The quantity of oil delivered per stroke is determined
by the width of the spacer between the two o-ring.
The order of the lubricator pump components as
delivered
Since I want the maximum oil flow for the first few steamings I
reassembled the pump with both spacers between the o-rings.
The new bracket worked very well and I didn't even need to adjust the
position of the delivery pipe. At the suggestion of David P I have
placed a fiber gasket between the cylinder and the bracket to reduce
heat transfer that might otherwise thin the oil reducing the efficiency
of the pump.
I am not totally happy with the geometry of the linkage and this will
need to be addressed.
Saturday: I had thought that I would have the extend the arm
from the valve gear upwards so that I could get the intermediate linkage
between
the valve gear and the lubricator arm horizontal but after
a lot of musing I decided that it did not matter if this linkage was at
an angle.
In the sketch right I show the position of the linkage at each end
and in the centre of the stroke. Provided the linkage is set so
that the lubricator arm swings equally about vertical the swing of the
arm will be the same as achieved with the intermediate linkage horizontal.
(Since the intermediate linkage at the beginning and
end of the stroke is parallel the horizontal distance moved by its ends
are the same) I have exaggerated the geometry so that the effect is clear. The
case shown is not practical as at the right had end of the stroke the lubricator
arm and linkage nearly come in line so putting excessive strain on the mechanism.
The grass is always greener on the other side On checking out the function of the new lubricator I discovered that
is was tricky to get sufficient motion when fully notched up to click
over one ratchet. I can now see the advantage of the original lubricator's
roller
clutches which, having no teeth, are capable of working with a smaller
stoke.
I have recently learned that ModelWorks have updated the design of
their lubricators to use 4mm roller clutches in order to ensure reliable
operation. Since the Burrell's lubricator is to this improved
design I might have been hasty buying a replacement.
Thursday 9th February: Last week I
received a letter from ModelWorks explaining that constructors would be
receiving new pistons as there was a concern that the rings could get trapped
in the ports. I suspect this was the source of Arthur's trouble
when he steamed his Burrell.
While I have have not yet received my replacement piston, Mike has, and
it is worth sharing what he found when he removed the old piston for
replacement.
The picture speaks for itself. Fortunately for Mike, damage was
confined to the piston and ring. It is particularly fortunate that
the cylinder bore was unmarked.
Given the seriousness of the problem the Burrell should not be
steamed or run on air until the piston has been replaced. It
is reassuring to know that ModelWorks have taken a proactive approach
and have already ship replacement pistons - don't put this one off - fit
the replacement piston! Mine has not yet turned up either it has
been lost in transit or ModelWorks are shipping them as they are
produced.
The problem arises because the length of stroke
of the piston causes the piston rings to pass over the ports at the side
of the cylinder. If the end of a ring get trapped in the port slot
it is shattered when the piston starts its return stroke.
The solution is the change the piston to one with only one centrally
positioned ring. This avoids the ring ever overlapping either
port. Since the Burrell's stroke is 97mm and there is 103.3mm of
unobstructed cylinder between the ports the centre 6.7mm of the piston
is never exposed to the port.
Friday 17 Feb: I have been musing on whether the piston trouble is
indicative of a more serious problem. In sort the answer is no but
I will also give the long winded explanation. It is clear that the
piston will partly cover the steam ports at the end of stroke and momentarily
impede steam flow. This lead me to check my Live Stem Models
4" Burrell drawing where I found very similar geometry. In
this design the port is eclipsed by 7/32" at the end of each stroke.
Clearly partial port covering at the ends of stroke is nothing to worry
about. To avoid the piston covering the port either the ports
would have to be made much narrower or the cylinder bore lengthen thereby
increasing the dead volume at the end of stroke. Both there two
option would have a much more serious impart on performance than the original
"problem".
The Cluputs are the culprits
The ModelWorks Burrell is fitted will Cluput
piston rings and I believe this improvement triggered the problem.
The Cluput rings consist of
two ring joined together. This means they are relatively fat but
more significantly have and addition edge.
As soon as the first half of the ring goes over the port it is liable
to spring out and become trapped. This is particularly likely if
the gap has rotated to be over the port. In the diagram on the
right have have tried to illustrate how this reduces the
"safe" stroke of the piston. In both cases the margin is
small and there is the addition complication that the boiler will
stretch when hot moving the piston towards the crank.
Today I fitted the new piston which has a single centrally mounted Cluput
ring. As instructed I removed the old piston by removing the
front cylinder cover. Curiously I found the piston rod easy to unscrew
from the cross head. The reason turned out to be that I had never
tightened the locking grub screws. We we told to leave these
lose when fitted during kit 11 and I can find no instruction requiring
them to be tightened. While it is obvious that they should be tighten
I could find no guidance on setting the piston rod length. An
overlong or short piston rod will exacerbate the problem with the piston rings entering the ports which perhaps explains
why some constructors have been badly affected.
I had expected to have great difficulty removing the piston rings and transferring
one to the new piston. In the end I found it easy to unwind them and refit.
What I was not expecting was the trouble I had getting the old piston off
the rod. The lock nut was easily removed but even with the rod
held in the vise and the piston gripped with a lathe chuck I could not
get it to budge. As I suspected Loctite I gently heated the piston
with my blowtorch. I guess I took the temperature to
around 160 C and at this temperature it unscrewed easily.
When I reassembled the engine I went to great pains to set the piston
rod length so that the piston sweep was central between the ports.
Having found this position I then slightly lengthened the rod to
allow for expansion of the boiler and did up the grub screws to lock the
piston rod in this position. Once I had refitted the end
cover I ran the engine on air and I was rewarded with a nice even
chuff.
Thursday 9 March: I plan to steam the
Burrell in the next few days and it preparation I have been giving the
engine a through check over.
In
correspondence with Steve Traill
I have been alerted to problems caused by the loosening of the
hornplate/boiler bolts. The boiler is secured using a M8 mushroom
headed bolt in a 10 mm clearance hole.
In an attempt to
resist sideways motion I made brass bushes to reduce the clearance
between bolt and hornplate. These bushes were custom made with the
hole offset to suit the alignment at each hole. Before
tightening the bolts I removed the paint from the side of the
hornplate.
In order to get at
the bolts it was necessary to remove the rear wheels
and gear guards. On seeing the differential exposed I was inspired
to have a go at getting the diff lock working properly. When I
visited Steve Traill I was surprised how freely his lock operated and he
explained that he had straightened the operating horse shoe. I
removed mine and checked it on my surface plate. Sure enough there
was a slight twist that was causing a fore aft twist of the
locking ring. I tried straighten this using brute force but this
caused the brazing to give way so I was forced to get out the brazing
torch.
Fitting
the upper gear guard is made very fiddly by the need to fit 4 nuts in
the inaccessible recess between the hornplate and the gears.
To overcome this I decided to make "nut bolts". In essence
these are M7 bolts with a M5 tapped hole through the centre. I
drilled out the hornplate and tender fixing holes, tapped them M7 and
then screwed the "nut bolts" in place.
The nut bolts are shown in close up on the right and may be seen
fitted to the hornplate in the shot above.
These
changes made refitting the upper gear guard very easy. When I
retested the diff lock it slid in very easily in sharp contrast to the
extreme force needed before.
When it came to fit the reach road I noticed that the bolts joining
the two parts had come loose again! Since it is difficult to get a
good grip on the M4 bolts I decided to replace these with M4 caps.
If they come loose again I will be getting the MIG welder out.
14/4/06: They did and out
came the welder. Saturday 11 March: I have been
contacted again by Steve Traill who has been working with Steve Baldock
to iron out the problems with the injector. It has transpired that
there is a design issue with the clack valves. There is excessive
lift in the boiler feed clack valves which can allow the ball to move such
that the feed to the boiler is blocked. Not only does this prevent
the injector working it can place excessive strain on the crank
pump. It is therefore advisable not to steam until this issue has
been resolved.
I
removed the feed pipe from the injector's clack giving me access through
the clack to the base of the ball. Using a nut and bolt as a depth
gauge I was able to determine the ball lift. I then removed the
top plug and by reinserting the bolt was able to see how far the ball
can lift before hitting the stop. As the picture on the right
shows the ball is lifted high enough to block the outlet to the
boiler.
Steve Baldock is aware of the problem and I am sure Modelworks
will be issuing a fix in due course but as I am keen to steam I decided
to have a go at my own fix.
The obvious
solution is extend the stop on the top plug. Rather than make new
plugs I drilled out the existing stop and threaded in a length of
1/4" brass. I then turned this to finished dimensions giving
a lift of 1mm for the crank pump and 2mm for the injector. Less
lift on the crank pump's clack is desirable as this reduces the tendency
of the ball to bounce between strokes.
The picture on the right shows the before and after for the injectors
stop.
I
have never filled the tender with water and in preparation for steaming I
filled this to the brim. This also gave me a chance to check out
the crank pump and flush the injector's pipes.
Sunday: I checked the weather forecast
for tomorrow and as it is sunny I will steam tomorrow. I spent the
day doing final checks and preparations.
I had
not applied any gasket sealer to the valve chest cover so this was one
of the jobs I tackled. When removed the cover I was engulfed in
tarry steam oil which had accumulated at the bottom of the chest.
Without the heat from the steam it was not all reaching the
cylinder. Had I not removed it I am sure in the first few stokes
on steam it would have been all over my drive.