Kit 22 - The penultimate kit
Continued
ModelWorks 4 inch Scale Burrell
Agricultural Traction Engine
Kit 22 was delivered Monday 19th September
I have started getting the items of Steve's shopping list.
Unfortunately my local Tesco has decided it is Christmas and replaced the
barbeque briquettes with Christmas puddings.
When I
brought water treatment from Live
Steam Models I also brought 1/2 metre of their 3mm PTFE gland
packing. It turned out to be square despite the catalogue saying 'dia'
(square is good!). I think this is similar to that
recommended by Steve. The packing from LSM works out at about the
same price as RS but you don't have to buy 8 meters.
So far I have only tackled the valve chest as it was
leaking badly. The way I fitted the packing was to wrap it
around the shaft and cut rings using a scalpel. You have to waste a
bit at the end so if possible cut all the rings that will be needed
for each shaft in one go. I managed to fit 3 rings into the
stuffing box offsetting the joints between each piece.
Over the next few days I shall remove the gear change
assembly for painting and permanently fit the water gauge. I have
found that this kit needs a lot of TLC (tender
loving care) and it is well worth spending the time to get it
right.
Friday 30th: Time
to stop hating the pipes and give them some TLC. When I fitted the
sight glass drain I found that I had a tangle of
pipes and I wanted to sort this out. Now that I have a former I am
able to bend the pipes whilst hard which has the advantage that they are less
likely to collapse. I
moved the bends of the water lifter's steam feed so that the pipe went the
other side of the feed to the injector.
In the picture right the blue felt tip shows the original position of the
bend.
The
result is a lot neater and I have also been able to arrange it so that the
pipes go out of the tender parallel one on top of the other.
The
bracket supplied was designed to support one pipe as it emerges in the
centre of the tender's slot. Clearly I could not use this bracket so I made a
new one. The photo montage right shows the new bracket at various
stages of manufacture. In a bar 1/2 x 5/16" I drilled holes for
the 3/8 & 5/16 pipes and them immediately milled off the top half.
I
considered this the easiest way of producing the moon shape recesses.
As I could not use the same holes to fix the support to the tender and for
the clamp plate I drilled and tapped 4 x M4 holes. Finally I made a
clamp plate from brass sheeting.
I
had no intention of totally rebending the pipe where it delvers steam to the
water lifter but when my attempts to get the original pipe to run parallel
to the top of the tender went awry I decided to have a go.
I completely straightened the "outside" portion of the pipe
(without annealing). As I could see I would have plenty of pipe
I cut off about 5" to have a trial go at forming the bends. This
went well but when I tried to do it for real I found it very difficult to
get the bends tight enough to arrive at the union.
In order to get
things compact enough I found that I had to run the two 90 degree bends
together ie. start the next before the first is finished. I had
a degree of success but I now fully appreciate why ModelWorks chose to route
the pipe the long way round. The original routing can be see in the
picture right (courtesy of Mike).
My final task was to sort out the water feed from injector to
boiler. I found that having bent the pipe so as to pass over the two
pipe supports it arrived at the injector 1" below the
union.
On
rebending the final kink so that it arrived at the union I found I had too
much pipe. Rather than muck around inserting addition bends to lose
the extra I opted for the drastic solution and cut off the excess.
My TLC may appear brutal but you have to be cruel to be kind!
Reverser Quadrant: Mike recently contacted
me concerning a problem he encountered after running his Burrell on
air. He was having trouble with the bolts that secure the two parts of
the reach road together coming loose. I to had this problem and nearly
welded them together before discovering the route cause. As it is clear many Burrells will be affected I think it is
time I wrote it up - so here goes.
12/4/06: In the end I got the welder
out!
Despite the new quadrant the die block is hitting the end of the expansion
link whenever full gear is selected. It only does this for part of the
stroke and there is enough give in the linkage for the engine to run
OK. Unfortunately the continual twanging of the reach rod causes the
bolts to come loose.
Even if the bolts could be locked the stress on the valve gear would be unacceptable.
The
is a simple method to check for and observe the extent of die block clashes.
Hold the reverser's ratchet open and
gently pull back on the reversing lever, it will probably go back beyond the
last notch. Now while maintaining gentle backward pressure on the reversing
lever turn the engine over by hand. You will find that the reversing level
rocks back and forward. If you look at this in relation to the notches you may
see that it comes forward of the last notch. When the lever is retained in
the 3rd notch instead of the lever moving forward of the notch the reach rod
will be stretched and the valve gear 'twanged'. Now repeat this with the
reverser full forward.
I
have discussed this issue with Steve and he wants to wait until a few
Burrells have been steamed before jumping to a solution.
As a interim measure I have optimised the length of the reach rod to
enable all three forward notches to be used without die block clashes.
To prevent damage to the valve gear I have Loctited a small cube of aluminum
to prevent selection of full reverse gear. I can now run the engine
for extended period without problems.
I was curious to see what effect this compromise would have one the valve
gear timing so I measured it using the same method I had before.
Perhaps I have written a clearer account for the POP
timing here.

This diagram shows the side valve position as a function of piston position
(percentage of full stroke).
0% is with the piston at the crank end and 100% the other end, 96mm
away. The valve position is in mm and I have ruled lines at +/- 4.8mm representing
the valve lap.
The red ellipses are the three available
forward gears and the two cyan ellipses
are the remaining two reverse gears. In forward gear cutoff occurs
at approximately 25%, 50% and 70% and in reverse at 45% and 70%.
The exact values can be read off the diagram where each ellipse cross the lap
line. Also note there is a small variation depending on the direction
of piston travel. The yellow line is locus for mid gear.
The results show excellent performance in forward gears with a useful
range of cutoffs available. In reverse despite the blanked off notch performance
is respectable. Given that many fully size engines have fewer notches
in reverse the final solution may well be to abandon the 3rd reverse slot permanently.
Wednesday 5 October: When I previously ran this engine I did this
without pressurising the boiler. Will most of the fittings fittings
supplied I decided it was time to pressurise the boiler. Rather
than connect the compressor to the cylinder I made an adaptor so I could connect
it to one of the clack valves. I did this to avoid blowing more muck
into the boiler.
With only about 10psi on the clock I was disappointed to hear a loud
hissing noise coming from below the crank. Tracking down the exact
source was difficult but the "soapy water test" implicated the
elbow on the right hand side of the boiler.
Access was difficult so I decided that the crank would have to come off.
I had been dreading removing the crank but in the end it came of quite easily
complete with eccentrics and gears.
I removed the pipe & elbow and carefully refitted it but it was no
better. With improved access I could feel a draft coming from the
pipe. I thought that somehow I had punctured the pipe but on removal
for testing in the time honored manner I discovered that it was leaking
from one of the fittings.
In the picture below left a small crack can be seen between the pipe
and the ferrule. When I removed the ferrule the failure of the
silver solider to penetrate can clearly be seen in the picture below
right.

Repairing the pipe was simple but now I have to repaint it (why didn't
I decide to leave them copper) and refit the crank.
Following a tip off from Mike I checked the cocks in the water gauge
for burrs. On disassembly I did indeed find small burrs left over
from drilling the passage. I removed these but unfortunately on inspecting
the valve seats I could already see that they were scored. Currently
I do not have the gauge glass fitted and leakage around these cocks is my
biggest remaining leak.
Saturday: Removing the burrs from the gauge cocks made them
worse. I presume that the burrs were actually helping to form a seal
in the scored valve seat. The original seat was made from a PTFE plug
screwed into the brass body. I like a challenge, had time to kill and
some PTFE bar.
My first act was to make a tapered D bit to cut the new seat.
Having successful completed a dummy run on a scarp of PTFE I grouched out
the old seat. I then plugged the hole with PTFE and bored the new seat
in situ. I then re-chucked the valve body so that I could re-drill the
passage. I finally fine tuned the depth of the seat using the D bit in
the pillar drill. Don't attempt this at home; ModelWorks are asking
customers to return any faulty water gauges for repair.
While
checking the installation of the gauge I found that when the upper gauge
cock was in its normally open position the operating lever hit the 2nd axle
tube. Visually inspecting the passage through the valve I could see
that the valve was not completely open (I had to remove the valve to see
this). The effect was made worse, in my case, because the passage was
not drilled at right angle to the handle. Since I was concerned that
this restriction could affect the operation of the gauge I put a dogleg bend
in the operating level such that when it was resting on the axle tube the
valve was completely open.
In addition to a drain valve the gauge has valves in the upper and lower
connections to the boiler. Prior to do some research I had assumed
that these valve were there in case of gauge glass failure - wrong -
they are there for testing correct gauge operation. It is possible
over time for the bores connecting the gauge to the boiler to become
blocked leading to false indications.
|
Water gauge test procedure |
| 1) |
Close the lower gauge valve then open the drain cock and blow the
glass clear |
| 2) |
Close the drain cock and open the lower
gauge valve. Water should return to the glass immediately |
| 3) |
Close the upper gauge valve then open the drain cock and allow the
water to flow until it runs clear |
| 4) |
Close the drain cock and open the upper
gauge valve. Water should return to the glass immediately |
|
If the water return is sluggish, the operation should be repeated. A
sluggish response could indicate an obstruction in the pipe connections to
the boiler. Any leakage in the water gauge fittings should be corrected to avoid
false indications. |
Wednesday 12th October: I have just learnt that Modelworks
are recalling the affected water gauges so that they can replace the valve
seats. Having replaced the seats myself I know this would be beyond
many model engineers. My advice is to take up ModelWorks generous
offer.
A thought: I am now running the Burrell with the boiler in circuit
and the power of the engine is awesome. Whenever the boiler is pressurised
treat the engine with respect - it could leap into life without
notice. Make sure hands are clear and it is out of gear. I learnt
my lesson the hard way with my Bodmers
Engine. It took me two years to build and I had grown accustomed
to resting my hand 'in the works'. The day came to set the valve gear
up which has to be done live. 2 1/2" dia piston, 60 psi, crank, thumb -
ouch. My rule now is to release all pressure before putting hands
into the works. I find the blower a convenient method for
releasing pressure.
|