Kit 22 - The penultimate kit
I find it hard to name this kit as it addresses
several functions
ModelWorks 4 inch Scale Burrell
Agricultural Traction Engine
Kit 22 was delivered Monday 19th September
Monday: Did not get much done as the kit did
not arrive until 5pm.
Tuesday:
Checking though the contents I noticed that the the long studs for the whistle
base have not been included. I have contacted Steve and they will be
included with the final kit.
I started with the pipes. I hate
pipes. I had hoped that fitting the pressure gauge pipe would be
easy but the corner under the pressure gauge is very congested. I had put
in additional kinks to get it to go behind the other pipes.
I
turned my attention next to the steam feed to the water lifter. When
I offered up the pipe It was about 2" too long at the joint near the
fire door. While I could have lost the extra by bending the existing
kink into an 'S' I decided to reroute the pipe completely so that it does
not obstruct the fire door.
I
straighten the the end section of the pipe in preparation for rebending.
As I needed to perform 90 degree bends I decided it
was time to make a former. I rebent the pipe so that it goes
down to below the op of the water tank before it comes across to meet the
mating
pipe. This routing used up the extra pipe - problem solved.
Where this
pipe exits the tender there is meant to be a support. Unfortunately
because of interference from the Injector steam feed pipe it is not
possible to fit this. I plan to make a combined support that will
use the existing fixing holes and support both pipes.
A final problem with this pipe was encountered when I tried to
connect it to the water lifter. The union nut is longer that the
threaded portion of the lifter with the result that it cannot be tightened
down onto the pipe's nipple. I will either have file down the union
nut or insert a packing washer. As I said - I hate pipes
Wednesday:
Today I fitted the gear change lever. When filling the locking plate
to size I quickly got it to a size that I could engage either gears but I
was finding that I was having to push the yokes by hand to get them out of
the way to swing the locking plate. At this point the instructions
made sense and further filling of the plate was required so that I could
be swing the plate given the positions the yokes where coming to rests. As
it says this needs to be done a little at a time. When finished
whenever the lever is returned to natural the locking plate has a clear
run to be swung into either position.
I did discover that it is possible to move the locking
plate whilst 2nd gear is engaged to a position that could allow 1st gear
to move. After a lot of playing around I did manage to engage both
gears simultaneously. First I had to stop the engine in just the
right place, engage 2nd gear and then push the interlock to one
side. It was then possible with a lot of jiggling of the gear lever to engage both gears
simultaneously. Any sensible movement of the gear change lever immediately
unmeshed 1st restoring normal operation.
While a theoretical possibility I conclude that this is
not a real problem.
Wednesday:
Fitting the blast pipe was relatively straight forward but I did find I
had to remove the cylinder studs. Now that I can see the finished
results I am glad that ModelWorks took the time to get it
right. The smooth lines have been achieved by bending two separate
copper pipes silver soldered together. Apparently the pipe bender couldn't
achieve the two bends close enough together.
The
water gauge was next. There is not a lot of room around the water gauge
and I wish it had been supplied with an earlier kit. The steam head
in particularly
got in the way when tighten the bolts. I found that by removing a
valve knob I could just about get the spanner in. Most of the
fittings have imperial heads and I am glad I invested is a set of imperial
AF spanners.
When I fitted the top gauge body I found that the mating
pipe was about 3mm too short. Too my surprise I found that it 'stretched'
when I did it up the unions. Don't worry as the pipe was kinked the
extra came for a change in geometry rather than actually stretching the
copper.
I found that once I had fitted glass bush, BU42232, I was
able to use a length of 3/8 diameter brass rod to check alignment with the
bottom gauge body. See picture right. It is well worth finding
something of 3/8" diameter as it takes the guess work out of alignment.
I found that I had to trim 1/16" off the lower water gauge
extension and a similar amount off the body in order to get it to go back
far enough to align with the top body.
Time
spent getting the alignment right was well worth it since I don't want any
strain being transferred to the glass when it is fitted.
When it came to fit the drain pipe I found it was very
close to other pipes. This was possibly made worse by my re-routing
of the water lifter steam feed pipe. When I get round to it I shall
try and take the water lifter pipe the other side of the injector steam
feed pipe.
The
final act was to fit the water gauge protector. I found in order to
be able to fit it I had to file the slot in the top plate so that it would
slip over the hex portion of the gland nut.
Unfortunately when I tighten the M3 locking screw it
caused the protector to tip forward. I hope that by judicious filing
of the bottom plate I will be able to correct this.
Time and patience are required to assemble the water gauge
but the results are well worth it. That's the dry run complete, now
I have to fit it permanently.
Friday:
Lapping the cylinder drain cocks proved problematic. Before starting
I could see significant patterning in the valve body left by the taper
reamer and one or two scratches.
After a modest amount of lapping I cleaned the valve and
tried it on my air line at 60 psi. There were leaks top and bottom
and surprisingly air escaped through the valve when shut. I
continued lapping and eventual got a good seal top and bottom but still
air escaped through the valve when shut. I deduce that the taper
widens out in the centre of the valve allowing air to pass around the
valve cock from inlet to outlet. By this time I was getting worried
as the hole in the drain cock was sinking below the line of the hole in
the valve body. To overcome this problem I used a dentist burr in my
mini drill to elongate the hole upwards. Since the cock now passes further
into the valve I had to make a packing washer to allow the nut to be
tightened.
I continued lapping and while the seal improved it still
passes a little air when closed. On the second valve I took my time and exercised
extreme care but the same sequence of events ensued. I hope the
valves will be sufficiently steam tight, perhaps they will fur on my hard
water.
Monday:
Having got the drains as good as I could it was time to fit them to
the Burrell. Space is very restricted and a dogleg extension is used
to connect to the cylinder.
While the drain cock cannot be fitted with the with the
extension attached it is well work following the advise in the
instructions and filling the oversize packing washer such that the valve
will tighten in the right place before attempting to fit to the
cylinder. I later found that I need all the length I could get
so be careful not to file too much away.
In
order to get sufficient room to fit the drain cocks in is necessary to
shorted the two studs immediately below them (red
arrow). Each stud needed to be shortened so that it was
level with the original nut (washer fitted). To improve appearance I
then slimmed the nut so that there was small amount of stud protruding.
Before fitting the drain extension it is necessary to fit
the cylinder cleading. I found that the bass band interfered with
the drain extensions and had to be trimmed. Again it is better to use more rather that less packing washers
behind the extension. This is to provide
clearance for the valve to clear the nuts pointed to by the red
arrows.
To
obtain sufficient clearance for the drain to screw in, it is necessary to
assemble them when they are within 1/4 of a turn of their final
position. Even so I needed to temporally remove the stud to the
right of the rear valve (green
arrow) to allow enough room to work. Perhaps this was
because of the problems I had lapping the valve that caused the stem to
protrude further below the valve body than intended.
When fitting the operating level found that it was necessary
to re-bend it to get it to fit correctly. In particular I had to put
a lot of 'twist' into the shaft just prior to the flat plate to get the
shat to move away from the valve gear's rear rod.

This page is getting quite large and this is a logical place to split into
part 2
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