Kit 21 - Steam Head & Water
Pump
ModelWorks 4 inch Scale Burrell
Agricultural Traction Engine
Kit 21 was eventually delivered on Friday 19th August.
Friday: For some reason I noticed that there was no 90 degree
elbow SP59031 and this inspired me to carefully check the contents against
the packing list. In addition to the pressure gauge pipe mentioned
in the covering note I found that the injector to check valve pipe BU42155
and water lifter pipe BU21159 to be missing. After a tip off from
Mike I checked the fasteners and discovered that the fasteners for the
Steam head BU42151 and the Water Pump Gland BU42134 to be missing.
I have spent the evening trying to fit the crankshaft gears. I
cleaned up the spines in the gears using a fine file which exactly fitted
in the slots. I was then able to get the larger gear to fit. I
was not so fortunate with the small gear. It jammed when it was only
partway on the shaft. I could not find where it was binding and so I
assumed it was on the splines. After further fettling of the slots there
was no improvement. I searched elsewhere for the problem and I began
to suspect that the bore in the gear was slightly too small for the shaft.
I measured the internal bore of the small gear and came to the
conclusion that it was slightly undersize at one end. I decided to
see if I could get the bore of the gear to run true in the lathe. I
mounted the gear in the four jaw and centred it using a dial gauge.
I then coated the inside of the bore with felt tip and advanced the boring
tool to the bore and various points along its length. Inspecting the
rub marks in the felt tip confirmed that I had indeed got the bore running
true. I was surprised I accomplished this so easily. I then
took one extremely light cut (1or 2 thou) and removed the gear to try on
the crank.
Its
fit was better but not perfect however I decided to call it a day as it freely moved over the outer portion
where it needed to operate.
With
hindsight it would have been better to either not fit or remove the splines
and check the fit of the gear on the shaft without the complication of the
splines. It would then have been much easer to test the fit of the gear and
file/scrap/abrade the offending part to size.
Saturday: The
next task was to fit the brake to the differential. M3 bolts
were supplied to fit the lugs to the brake band but no nuts. I think the lugs were meant to be tapped M3 but I found
the bolts just about long enough to use nuts.
Before painting this assembly I decided to test the brake.
I found that with the brake at its limit of travel it was nowhere near griping. To
assess how much the brake band needs shortening I temporally shortened the
brake band as shown in the picture right.
In
order to get the brake to bite I had to treat both ends. This
measure shortened the band by about 1/2 inch. The picture right
shows the point where the brake begins to bite. Noting that the mechanism
will not clear the bottom of the brake wheel bracket it can be seen that
there is little to allow for wear of the cork band. In light of this
I am considering shortening the band by 0.6 inches. (23/8/05) Don't
shorten thicker cork is being supplied.
Sunday: Not
much time spent on the Burrell today. I did get a chance to fit the
blowdown valve. This has been supplied with a blanking plate to account
for the variation of alignment. see
I also made a start on the steam head but as the fixing screws are
missing I did not get very far.
Monday:
I found some long bolts which enabled me to temporally fit the steam head
(top holes only). I was pleased to discover that on refitting the spectacle
plate that the steam pipe fitted nicely.
Assembly of the water pump was straight forward and it was only when I
fitted it to the hornplate that I encountered a problem. I found
that the pump rod was out of alignment by about 1/16 inch on the
"vacant eccentric". I thought of bending the pump rod but
realised that since I had already permanently fitted it to the piston
there was no satisfactory way of gripping it.
In
desperation I tried rotating the pump rod through 180 degrees and to my
amasement found it now aligned perfectly. On inspecting the
connecting rod I could see that the holes were not drilled
centrally. As I don't know whether this is a lucky accident
or by design I would recommend trial fitting the pump before locking
the piston to the connecting rod. 11/9/05 also see below
The were
a lot of burs within the check valve casing and I spent some time
carefully removing these. The ball valve seat required special
attention as it is important that it has perfect edges. If found
that passing a 1/4" reamer in from the top did the trick. I achieved
nicely defined clean edges.
I have made a start fitting the pipes. Unlike the POP Modelworks
have supplied the pipes pre-bent. It took a while to figure out how
to fit the
injector steam pipe BU42154 as the ISO is "taken" from a strange
angle that makes the vertical portions disappear. BU42154 has been
supplied in two parts to enable it to be threaded into position without dismantling
the Burrell. Amazingly it
fitted without any rebending. Note: The top section looks like it would
fit either way round but I discovered that only one way was
"perfect". I am not having so much luck getting the pipes
to line up with the pipe supports. The injector water feed pipe
BU42156 is a tad too short. Rather than put a joggle in the steam
pipe I plan pack the joint with the water valve to "lengthen"
the feed pipe. The Pump to check valve pipe BU42158 completely
misses one of its supports. Since I am missing the elbow that
connects it to the pump I will not attempt to adjust the pipe until it is
fixed at both ends.

Tuesday:
When I tried to fit the water feed pipes to the pump I found both to be
1/4" too long. Rather than attempting to lose the extra by
bending the pipes I cheated and shorten them by 1/4". Mike has
managed to fit these pipes but he had to anneal them in order to get them
sufficiently pliable to bend.
Included with this kit was a replacement crank pin. By the look of it
has been hardened to reduce wear. It only took a few minutes to
clear up with a wire brush and fit.
Without the missing items from Modelworks this kit is grinding to a
halt. The only job available is to prepare the pressure gauge for
fitting to the spectacle plate.
STOP PRESS I have just heard from
Steve that there will be a mail out of the missing fasteners tomorrow.
The long pipes are to follow with the next kit - it seems they did not fit
in the box!
Thursday: Today I received the missing fittings from
Modelworks. This enabled me to fit the elbow to the water pump and
check the fit of the final pipe. While it lined up with the water
pump and check valve it completely missed one of its supports.
Bending the pipe to pass the support while still arriving at the pump
would require the top bend to be moved down the pipe by about two
inches. I tried straightening top bend but it didn't feel like it
wanted to go so I decided to anneal it. I heated the portion of the
pipe from the old bend down to the position of the new bend to a dull red
using my brazing torch and left it to cool (cooling rate is immaterial,
the important part of annealing copper is to heat to dull red). The change
in the pliability of the copper was dramatic and I had to be very carefully
when applying even moderate force not to wreck the pipe. Care is
also needed when manipulating the un-annealed sections of pipe that their stiffness does not cause the softened positions of pipe to bend
unintentionally. All this said, it did not take me long to get the
pipe to fit; now all I need to do it to find a way of hardening it
again.

Before and After
I have
been kept occupied these last few days preparing the many brass parts for
painting.
Looking at my picture collection I could not establish a consensus as
the which fittings would normally be painted. In the end I decided
to paint virtually everything as it is relatively easy to remove the paint
from any that I later decide should be left unpainted.
Friday: I finally got round to etch priming after spending 3
days on preparation.
Saturday: I painted everything gloss black using a high heat
paint.
Sunday: Fortunately the paint was sufficiently dry to commence
assembly. I started with the brake as this had the prospect of
enabling a lot of left overs from previous kits to be permanently fitted.
Modelworks have recalled the brake shaft and screw so that they can
silver-solder the two parts together. Not wanting to be held up I
did this myself. I experimented with the cork and found that using
both the thick and thin band together did not allow the brake to
be released. As a result I just used the new think cork however the brake
bites close to the limit of its travel and may spell trouble later on.
My
next task was to permanently
fit the rear spectacle plate. The four holes at the bottom needed to be deeply counter sunk
and the steam head fitted before fitting to the Burrell. I had to
substitute longer M3 screws when fitting the pressure gauge.
It would have been better to
have fitted the spectacle plate before fitting the brake thereby enabling
the differential to be slid out. This made access to some of the bolts difficult.
22/9/05 Consider fitting water gauge if available. See
The part I
most wanted to fit was the upper gear guard as this would enable me to get
the valve gear going again. This was very fiddly and it is a shame
that ModelWorks did not tap the hornplate holes M5 thereby
dispensing with the need to fit nuts. I also had to substitute some
of the fixing with longer bolts. I was also able to check out the
new reversing quadrant and was able to get all notches to engage without
any problems with the die block hitting the end of the expansion link. (11/9/05)
I am not confident that this statement is correct. When I attempted
to set the valve gear up correctly I again experienced clashes.
(30/9/05) I now know I have a problem with the
new quadrant which is described here.
Monday: When
the pump is fitted access to the 2nd shaft's oiler will be difficult but
possible. ModelWorks have supplied a 90 degree grease nipple to
replace the oiler but I would prefer to retain the original oiler.
I have seen many model traction engines where the oil reservoir is
remote from the axle and I decided to do the same. It was a easy job
to turn up two adaptors to enable the a section of 1/8" diameter copper
pipe to be inserted between the oiler and the shaft.
Tuesday:
When I came to fit the injector's steam feed pipe I discovered that it
clashed with the reach rod. When I previously checked the fit of
this pipe the problem did not show as the valve gear was not fitted. Now that I had painted
the pipe I discovered it did not fit!
To clear the reach rod the bend would need to be moved about 1/2"
closer to the globe valve. This was not going to be easy as the bend
had to start as soon as it leaves the fitting.
As I would be bending the pipe by
hand I annealed the top
of the pipe . Had I had
suitable bending formers I would have preferred to have left it hard as I
had great difficulty in preventing it collapsing.
I have now got the pipe to fit but it will have to be repainted.
Saturday 10th September: I have beefed up my compressor and have
been running on air again. The method used to plug the holes and
connect up the compressor is described here.
As a result of having more air (15cfm) the engine runs faster but this has
highlighted some problems. After a few minutes I noticed that the
lower valve eccentric was getting quite hot. I stopped the engine to
investigate. I found that the eccentric rotated freely except
for one or two slightly tight spots. I introduced more packing into
the eccentric strap but even with a total of 30 thou of packing the
eccentric was still running hot. Inspecting the inside bearing
surface of the strap I could see a band of what look like rubbing but on
closer inspection this turned out to be a raised ridge. I had
wondered whether prolonged running would fix the problem but Steve advised
me that if a bearing is running hot it will eventually seize.
Since add packing afforded no relief I decided to take the drastic step of
using valve grinding paste. I reassembled the eccentric with some
fine grinding paste inside and gave the engine a short run. I
then spent the next half hour scrupulously clearing the eccentric to
remove all traces of the paste. On reassembly I could
immediately see an improvement as the engine ran much faster.
After another extended run I observed that while the valve eccentrics
were running cold the pump eccentric was getting warm. I
checked out the eccentric and found that it rotated freely. Baffled
I tried running the engine without the pump eccentric and found that it ran
even faster. This proved there was a problem with the pump eccentric
but where was it? I tried shimming the strap to no avail and
when the valve lapping paste did not improve matters I was ruining out of
ideas.
Careful
inspection of the eccentric strap showed signs of polishing on the sides
which led me to wonder whether the strap was being twisted. The only
way to be sure was to remove to pump casing so that I could check the natural
position of the pump ram - was the pump bore pulling the ram sideways? In order to make a precise measurement I
found just the right thickness of packing to just fit between the ram an
the hornplates. I ended up with a 1" block and two 20 thou
shims (total 1.040"). On my surface plate I measured the equivalent
dimension on the pump at 1.100". No wonder it was rubbing it was
being pulled sideways by 1/16 ".
Live by the sword die by the sword
This
problem is largely of my own making. In order to get more room for
the eccentrics I machined a slice off the governor pulley. This has allowed the
pump eccentric to be fitted closer to the hornplate. Unfortunately
the room has now been used up and without major surgery I cannot simply move
the eccentric away from the hornplate. The correct course of action
is probably to put a crank in the pump rod but I chose a more drastic
solution! I would shave 60 thou off the foot of the pump thereby
moving it closer to the hornplate. I did this with the aid of my mill
plus fly cutter - I didn't even scratch the paint.
On reassembly the eccentrics ran cold but the engine did not run quite
as fast due to the additional load of the pump. Turning the engine
over by hand was now quite easy. The only significant resistance
coming from the piston as it pushed air through the cylinder. The
engine has lost it's 'bark' as the exhaust air is coming out at a much
lower pressure. While this does not sound as dramatic it is good
news as it demonstrates a significant reduction in friction. The
engine now only barks when accelerating the flywheel up to speed.
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